Hello,
I'm trying to setup UC400ETH controller and get strange results.
Jog movements are fine,
single line G0 code execution seems to work,
G1 X100 F500 command does actual movement with 2 seconds delay (DTG value is increasing first, then movement starts and X value is changing on the screen)
Run of G code file does only 1st movement, then no actual motion is going on until file stops.
See my screen video -
https://youtu.be/P1tqeovH1N0
I'm using latest 1.2042 software
the controller is connected via switch to local network.