Hi guys, this is my first post.
Bought 2 DG4S drives a month ago and just installed then. They seem to perform well, fast, precise, easy to set and install, powerful, but the PID control has a problem that manifest itself more on high resolution encoders, fast motors with low inertia and high voltages.
I made a video to display clearly the problem and hopefully be part of the fix.
https://youtu.be/LNMlm0xzmdI
It is quite a big dealbreaker since this problem makes the motor always shake when stalled.
A short description of the problem is that the proportional gain on the drive has a dead band where it does not output any power, then it outputs full power like if it was cumulating output but it did not translate into a real output power. So in this band the motor gets unstable whiteout an unstable PID loop which makes it impossible to make the motor settle. All the belts and ball screws and encoders are properly coupled with no meaningful slack or play.
I think this drive has an huge potential when it comes to machine retrofit and many other applications but this is a significant problem that limits the drive usefulness.
If I can help in any way to fix this I will be happy to be of service.