Hello all,
we are having the following issues: depending on "linear error / linear addition" values some arcs (G2 and G3) go completely wrong when Feedrate is at around 3000mm/min.
Even worse, hitting stop or pause button while the machine is in the wrong position, cause a rapid of the machine to the previous ( sometimes) next point in the Gcode: in our case the rapid is 20.000mm/min
This is enough to snap the endmill and creates a safety problem as the machine moves unexpectedly after the stop command.
I have videos and files available for testing.
Thanks
Giorgio