Hi everyone,I’m facing the following issue:
my machine has a clear “thud” or “hick-up” when M10/M11 commands are issued.
- the motion is along only one axis, X
- the X axis has a slaved motor (gantry), slaved through SW (Mach3)
- the Gantry runs smoothly up to 15’000 mm/min (ballscrew limit)
- whenever an M10/M11 command is issued, I can hear a clear, single thud (almost as it hit something)
- happens at all speeds I checked (from 1000 to 15000 mm/min)
- many times the two motors go out of sync and the gantry gets stuck
One way to solve it would be to remove M10/M11 and replace them with “normal” macros (stopping the motion every time an output needs to change state), but I would still like to know if you have any idea about how to solve it.
The configuration is the following:
- uc300-eth
- leadshine EM705
- stepper motor, 2Nm
- PSU 20A@48V
- Mach3
If needed, I can post the part of the code causing the problem.
Any help or hint would be really appreciated
Pietro